THE FINAL RESULT
My substantially more mechanically inclined friend and I took it all apart and installed the Maxxair Mixture screw. We found the
main jet was a 175 and the Baron needle was on the fifth position. We installed the 167.5 jet and put the needle on the third position. In addition we ported the manifold. Also the accelerator pump was turned all the way off and the mix was about 3 1/4 turns out.
Now the bike starts right up and really runs sweet! The initial milage estimate is 34 MPG. This is a slight improvement but what I really like the way that the bike starts up easily now with the charcoal canister removed.
One issue I have is the choke now will not stay out like it used to. Is there a special trick to that deal?
Also, I one other small issue is that there is a vent on the top of one of the corners of the cylinder heads, this has a tube that enters the air cleaner (
BAK). Often times oil get's puked out into the air cleaner, which causes it to get plugged up a bit and discharge oil out onto the pipes.
I really appreciate the help from y'all and a big shout out to the
Fauxrider who did the technical work.
THANKS!!!